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Valve Description: #1 Unit Feedwater Regulator Bypass Valve (MOV)

Valve as found: Original Info: Actuator / New Info:
Manufacture Republic Flow Meters Limitorque Gear box
Size 8"x 8"x 8" Model: L120 - Size: 420
Type Globe Solid stem / disc assembly, post-
guided, control valve. Single seat
Pressure 1500 Lb, Pressure Class  
Body Material WC6, Steel (1-1/4 % Chr.)  
Fig.# DRW# 5000-32-8  
Seat Material Stellite #6 (per provided drawing) 309L-SS / Stellite-#21 Overlay
Stem Material CR-13 Stem Diam. 2" Acme 4-TPI SL LH
Disc Material CR-13 (repaired in past) 309L-SS / Stellite-#21 Overlay
End Connection Butt-weld Schedule - Not Shown Likely Schedule - 160
Electrical Disconnect Yes  
Insulation No Hot Work Permit Required For Heating Or Welding
Scaffolding No  
Gasket Info (2) Required upper and lower bonnet Style: flat steel 7.250" x 8.437" x Th. 1/16" Manufactured by TFSG
Stem Packing Information (style & cross section) Found 14 Rings of Rope Packing Replacement - Garlock 1303 Cross-section 1/2" x 1/2" 5 Rings.

Problems found:
 
Seats:
 Evident leak through past seating surfaces, possibly causing flow control problems for the adjacent regulating valve. (Debris was found in upper and lower guide bushing of valve body.)
 Severe cuts found on Disc and Seating Surfaces.
 
Stem:
 Minor pitting in packing area.
 Upper Guide Post had severe gouges and galding caused by fractured weld of adapter plate at weld joint of bonnet / adapter plate. (This two piece construction was not shown on station supplied drawing.)
 
Bonnet:
 Bonnet / Adapter Plate weld joint fractured approximately 60% of the total circumference causing actuator adapting plate to bend approximately .140". Possibility of incorrect torque setting on Limitorque actuator.
 Upper Guide Bushing mirrored damage from upper guide post of stem.
 Depth of Packing Box on Bonnet is unacceptable but common for this vintage of valve. Appearance of possible packing leak. Depth adjustment required.
 
Gear Operator/Actuator:
 Stem - drive nut shows minor wear on acme threads. However, acceptable for continued use.
 
Body:
 Acceptable. (No evidence of cavitation or Body Damage.)

Corrective Action:
 
Seats:
 Removed old seat ring from valve body, manufactured and installed new seat ring.
 Removed approximately .400" total from diameter of disc by means of machining.
 Applied .200" of 309SS re-machined.
 Applied .200" Stellite21 hard-surfaced material. Finish machined to proper configuration and dimensions.
 
Stem:
 Check the T.I.R., found to be acceptable (.002" Run Out)
 Polished the packing area and lower post guide surfaces.
 Weld repair were made on upper guide post where gaulding had occurred. Weld repairs were made with 309SS; Upper guide post was then machined and polished to finished diameter of 2.604".
 
Bonnet:
 Separated adapter plate and upper guide bushing from bonnet.
 Re-Machined both sides of adapter plate for a 98% clean-up.
 Machined away remnants of old weld material from adapter plate leaving area for new weld material to be applied during construction.
 Fit and re-assembled adapter plate and valve bonnet applying 3 passes of 3/32" 8018 around circumference of point of attachment.
 Manufactured and incorporated 4 triangular gussets equally spaced 90° apart for additional strength as part of the bonnet / adapter plate reconstruction.
 Machined the nut shoulder surfaces to remove gaulding marks from bonnet nuts (97% Clean-up)
 Manufactured the new upper guide bushing from A105 Carbon steel pipe with 309SS / Stellite21 overlay on contact surface. Installation was .002 pressed fit with 4 tack welds.
 Manufactured new packing spacer to allow for proper compression of 5 ring packing set.
 New flat steel gaskets were manufactured to replace upper and lower bonnet gaskets.
 
Body:
 Body was thoroughly cleaned; Valve was re-assembled and checked for smooth operation and proper alignment.
 After unit was brought up on load TFSG tech hot torqued bonnet bolts and packing in conjunction with a visual inspection for leaks or problems. None found.
 
Recommendations:
 Factory maintenance recommendations for Limitorque, motor operators are mostly based on: number of cycles, temperature, severity of service, torque, or limit settings and other sizing characteristics.
 It is TFSG recommendation that routine maintenance be performed on this motor operator at earliest opportunity.
 Although the valve was hot torqued after start-up, periodic packing adjustments and visual inspections are recommended every 3 months. This can be done by station maintenance personnel.

Special Tool Fabricated For Removal Of Actuator

Removal Of Actuator

Lower End-Cap As Found

Lower End-Cap Stem Guide Bushing As Found

Initial Inspection After Removal Of Lower End-Cap Reveals Debris And Areas Of Wash-Out Between Disc And Seat Ring. This May Also Indicate The Presence Of Debris Downstream And May Affect Other Valves Associated With This Line.

Removal Of Yoke

One Piece Disc And Stem As Found

Upper Guide Post As Found

Seat Ring In As Found Condition

Seating Surface Of Seat Ring - Damage Shown

Bonnet And Actuator Adapting Plate As Found

Packing Box Had 14 Rings Of Packing - 5 To 7 Rings Is Generally
Considered To Be Acceptable For Proper Packing Compression

Upper Stem Guide Bushing As Found

Upper Guide Bushing As Found

Gasket Area Of Bonnet As Found. Gasket Area Appears To Be In Good Condition.

Yoke In As Found Condition - Evidence Of Packing Leak On Lower Side Of Yoke

Miscellaneous Parts As Found

Removing Weld From Adaptor Plate - Previous Weld Did Not Achieve
Proper Penetration To Maintain Bond. (This Was An Unsatisfactory
Design Change To The Original Equipment.)

Actuator Adaptor Plate Removed From Bonnet

Inspection Of Actuator Adaptor Plate - Plate Bent .14"

Upper Guide Bushing Removed

Material For Fabrication Of New Upper Guide
Bushing (2" Schedule 80 Grade 217 A-105)

Machine Prep For Stellite 21 Overlay To Upper Guide Bushing

Applying Stellite 21 Overlay To Contact Surface Of Upper
Guide Bushing. (Overlay thickness - .125" Per Side)

Machining Of The Stellite 21 Overlay On Upper Guide Bushing

New Upper Guide Bushing Installed And Secured
To Bonnet (.002 Pressed-Fit And Tack Welded)


Removed .14" From Surface For A 98% Cleanup Of Plate

Machining Bonnet In Preparation For Adaptor Plate

Attaching Adaptor Plate To Bonnet

Welding Mounting Plate To Bonnet

Adaptor Plate And Bonnet Prior To Installation Of Upper Guide Bushing

Seat Ring After Removal From Body - Seat Ring Did Not Have A
Locating Shoulder As Represented In Drawing Supplied By Plant

Material For Fabrication Of New Seat Ring
A36 Carbon Steel Plate 2" Thick 8.5" x 8.5"

Fabrication of New Seat Ring - 309SS / Stellite 21 Overlay On Seating Surface

Finished Seat Ring Ready For Installation

Welding New Seat Ring Into Valve Body

Inlet Side Of Seat Ring After Installation

Solid Disc And Stem During Inspectin - T.I.R. - .002" Diameters Appeared Original


Old Seating Material Being Removed In Preparation For Weld Build-Up

309 SS / Stellite 21 Weld Overlay Prior To Final Machining

Weld Repair To Upper Guide Post

Final Machining In Progress

Final Inspection After Repairs

Original Gaskets

Stock For Fabrication Of New Gaskets (A36 Carbon Steel)

New Gaskets

Final Assembly

Final Assembly

Complete And Ready For Service


**Addendum**

Customer Requested Installation Of Control Unit. Following Is A
Pictorial Documentation Of Requested Installation

Attaching Level Control To Line

Installation Of Gaskets

Level Control Complete


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